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Overview
Oct 29, 2016
Oct 12, 2015
Jun 20, 2015
Apr 25, 2015
May 11, 2013
May 27, 2012
Nov 5, 2011
Oct 9, 2011
July 28, 2011
June 11, 2011
Nov 6, 2010
Aug 21, 2010
June 12, 2010
Nov 7, 2009
Oct 11, 2009
May 30, 2009
Nov 8, 2008
Oct 12, 2008
Jun 14, 2008
Apr 13, 2008
Oct 27, 2007
Oct 8, 2007
Jun 10, 2007 - Excav.
Jun 9, 2007 - Second
Jun 9, 2007 - First
Nov 5, 2006
Sep 1-2, 2006
Jun 10, 2006
Jun 10, 2006 - Tools
Nov 4, 2005
Sep 1, 2005 - CanIron V
Jun 11, 2005
May 14, 2005 - OABA
Jan 14, 2005 - Consolid.
Oct 24, 2004
Jun 3, 2004
Jun 3, 2004 - Design
Jun 3, 2004 - Questions
May, 2003 - Analysis
May 2003
May 2002

Iron Smelt - Laurel, ON - Oct 29, 2016

Date:Oct 29, 2016

Location:Laurel, ON

See also: Darrell Markewitz's ironsmelting site

Team: Richard Schweitzer, Darrell Markewitz, Neil Peterson, Vandy Simpson, Eric, Brandon, Nathan

Premise: Return to the Icelandic (Háls) series.

Furnace Design

TypeIcelandic Turf construction with clay lining, tap arch
Extractionbottom
Diameter0 cm
Height0 cm
Volume0 cm3
Tuyure Typecopper tube
Tuyere height from base0 cm
Tuyere penetration into furnace0 cm
Tuyere angle0 deg
Base designnatural set base cm

Burn Details

Bellow Typeblower
Avg Air rateest. 1000+ litres per minute
Total Charcoal Mass0 Kg
Avg Burn rate0 min per 2 Kg
Ore TypeDD1+
Total Mass of Ore0 Kg
Burn Duration0 Hours

Results

Mass of Bloom2.5321 Kg
Bloom Type0
Yield0%
Notes0

Smelt_cd Reports of all of our iron smelting efforts along with more articles and information are available on the "Iron Smelting in the Viking Age" CD from the Wareham Forge.  Copies of the CD can be purchased here.

Discussion:




Conclusions:


There were several concerns that were evident before the smelt even started -- and all of them became issues.
  1. A full bag of powdered clay proved to be insufficient and the 3 cm thick wall topped out at 60 cm. This meant that the top 30 cm was only turf. It was also wider as it was left with the assumption that clay would be acquired later. As the organics of the turf burned away, this top section gradually eroded and took on a cone shape. This not only put more dirt (silica) into the smelter and increased the slag, but it also may have affected where the ore fell in the shaft.
  2. The weather in the preceding week was wet and cold, with 5-10 cm of snow falling mid week. It was warm on the Friday, which helped, but with the damp the clay liner (which hadn't been completed as early as planned) had no chance to dry. As a result, there was massive spalling right from the start during the pre-heat, even before we switched to the charcoal. Twice we opened the bottom to remove partially slagged ceramic material. Fortunately, this was before we had started adding ore, but even after, it took a long time before things stabilized. Two more times we had to open up the bottom to try to lower the bowl and/or tap the slag. We also were constantly battling to keep the tuyere clear as slag froze over the opening. As a result, there were multiple interruptions or reductions in the air flow.
  3. During construction, things shifted and the round cylinder turned into more of an oblong, egg shape. This may have increased wall erosion as the narrow edges near the tuyere were the damaged first. This may also have been a factor with our air. Despite the blower running fully open (a first for a DARC smelt), the blower didn't seem to get full penetration.
  4. The soil in the area is very sandy. This seems to have created several problems. Firstly, the grass root mass penetrated deeper into the soil, but without much density. This lead to some structural issues during construction, and there were real concerns of the exposed front wall collapsing during the smelt. Secondly, there was no sintering of the soil which might have happened if there had been a higher clay content. Concerns over structural integrity led to a log and later a pipe being added, along with several sod blocks, but the threatened collapse of the front never did materialize. Much of the credit goes to the stone lintel over the tap arch which played a big role in stabilizing everything as we fought with the slag. The addition of extra sod blocks at the bottom did a good job of controlling unwanted jets of flame without too much extra effort, with the added bonus of being easy to remove when necessary.
In the end, the degradation of the smelter made a front extraction a foregone conclusion. Adjusting the air hoses out of the way was the only tricky step, and that was minor. When the smelter was opened up, the bloom was retrieved easily and quickly moved for consolidation.

The bloom was a bit smaller than usual, but the smelter still needs to be investigated for other bloom material and "gromps" (iron bearing slag).

The copper tuyere worked exceedingly well. Care was made to keep as much of the copper exposed to insure that it could radiate the heat efficiently, but despite the issues during the smelt, it didn't seem to show any sign of wear.

The wooden crib was not affected by the heat until the extraction, at which point the short sections that were angled in toward the tap arch began to smoulder. Clearly the 90 cm gap was just about perfect -- any narrower, and the crib might have caught fire, any wider and it would have been too wide to reach over to add ore and charcoal.

The stone lintel over the removeable block worked well. We accessed the interior several times without destroying the smelter. However, concerns over the sod immediately above the tuyere suggest that the sod there might be better replaced with more stone, or with a wider foundation for the sod at that point (a second lintel above the tuyere?) .

The emergency wooden support log lasted surprisingly well considering it was dry cedar. As it didn't burn through until the bloom was pulled, this suggests that green hard wood poles could work to make a base for a wider front wall above the tuyere.

The profile ended up much flatter than the 45 degree angles shown in Smith's reconstruction. However, the space seemed to work fairly well. Whether it works as well with bellows remains to be seen.



Photos:


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Wooden frame Cut Sod Tap Arch First layers
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3 layers finished Clay lining Lining pulling away Clay wall
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clay lining Overview From the top Leaking flames
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Fun View Slagged walls Tapping Running Slag
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Lots of slag Collapsing top Vanishing walls Bloom bits
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Aftermath Erosion Wall Remains Large bloom

Raw Data:



CLOCKELAPSEDEVENTAIRCHARCOALORE
UNITCOUNTTOTALADDTOTAL
gateLpMbucketkgKgkg
Smelt_cd Reports of all of our iron smelting efforts along with more articles and information are available on the "Iron Smelting in the Viking Age" CD from the Wareham Forge.  Copies of the CD can be purchased here.
Text © Darrell Markewitz
Photographs © Darrell Markewitz
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